This is a timeline of what happened to the Chernobyl nuclear reactor that started on 4/25/1986 causing the worst man-made incident ever(so to speak). Although I left out wait happens in the surrounding area and people; look them up!
To this day, 30 years ago in the city of Pripyat, then located in the Ukrainian Soviet Socialist Republic of the Soviet Union (USSR). The Chernobyl nuclear reactor was doing test on it's steam turbines. During steady state operation, a significant fraction (about 7%) of the power from a nuclear reactor comes not from fission but from the decay heat of its accumulated fission products. This heat continues for some time after the chain reaction is stopped (e.g., following an emergency SCRAM[Basically a shutdown]) and usually requires active cooling to avoid core damage. RBMK reactors, like those at Chernobyl, use water as a coolant. Reactor 4 at Chernobyl consisted of about 1,600 individual fuel channels; each required a coolant flow of 28 metric tons (28,000 liters or 7,400 U.S. gallons) per hour.
Since cooling pumps require electricity to cool a reactor after a SCRAM, in the event of a power grid failure, Chernobyl's reactors had three backup diesel generators; these could start up in 15 seconds, but took 60–75 seconds to attain full speed and reach the 5.5-megawatt (MW) output required to run one main pump.
To solve this one-minute gap, considered an unacceptable safety risk, it had been theorised that rotational energy from the steam turbine (as it wound down under residual steam pressure) could be used to generate the required electrical power. Analysis indicated that this residual momentum and steam pressure might be sufficient to run the coolant pumps for 45 seconds, bridging the gap between an external power failure and the full availability of the emergency generators.
This capability still needed to be confirmed experimentally, and previous tests had ended unsuccessfully. An initial test carried out in 1982 showed that the excitation voltage of the turbine-generator was insufficient; it did not maintain the desired magnetic field after the turbine trip. The system was modified, and the test was repeated in 1984 but again proved unsuccessful. In 1985, the tests were attempted a third time but also yielded negative results. The test procedure was to be repeated again in 1986, and it was scheduled to take place during the maintenance shutdown of Reactor Four.
The test focused on the switching sequences of the electrical supplies for the reactor. The test procedure was to begin with an automatic emergency shutdown. No detrimental effect on the safety of the reactor was anticipated, so the test program was not formally coordinated with either the chief designer of the reactor (NIKIET) or the scientific manager. Instead, it was approved only by the director of the plant (and even this approval was not consistent with established procedures).
According to the test parameters, the thermal output of the reactor should have been no lower than 700 MW at the start of the experiment. If test conditions had been as planned, the procedure would almost certainly have been carried out safely; the eventual disaster resulted from attempts to boost the reactor output once the experiment had been started, which was inconsistent with approved procedure.
The Chernobyl power plant had been in operation for two years without the capability to ride through the first 60–75 seconds of a total loss of electric power, and thus lacked an important safety feature. The station managers presumably wished to correct this at the first opportunity, which may explain why they continued the test even when serious problems arose, and why the requisite approval for the test had not been sought from the Soviet nuclear oversight regulator (even though there was a representative at the complex of 4 reactors).
The experimental procedure was intended to run as follows:
- The reactor was to be running at a low power level, between 700 MW and 800 MW.
- The steam-turbine generator was to be run up to full speed.
- When these conditions were achieved, the steam supply for the turbine generator was to be closed off.
- Turbine generator performance was to be recorded to determine whether it could provide the bridging power for coolant pumps until the emergency diesel generators were sequenced to start and provide power to the cooling pumps automatically.
- After the emergency generators reached normal operating speed and voltage, the turbine generator would be allowed to continue to freewheel down.
The conditions to run the test were established before the day shift of 25 April 1986. The day shift workers had been instructed in advance and were familiar with the established procedures. [A special team of electrical engineers was present to test the new voltage regulating system.] As planned, a gradual reduction in the output of the power unit was begun at 01:06 on 25 April, and the power level had reached 50% of its nominal 3200 MW thermal level by the beginning of the day shift.
At this point, another regional power station unexpectedly went offline, and the Kiev electrical grid controller requested that the further reduction of Chernobyl's output be postponed, as power was needed to satisfy the peak evening demand. The Chernobyl plant director agreed, and postponed the test. Despite this postponement, preparations for the test not affecting the reactor's power were carried out, including the disabling of the emergency core cooling system or ECCS, a passive/active system of core cooling intended to provide water to the core in a loss-of-coolant accident. Given the other events that unfolded, the system would have been of limited use, but its disabling as a "routine" step of the test is an illustration of the inherent lack of attention to safety for this test. In addition, had the reactor been shut down for the day as planned, it is possible that more preparation would have been taken in advance of the test.
At 23:04, the Kiev grid controller allowed the reactor shutdown to resume. This delay had some serious consequences: the day shift had long since departed, the evening shift was also preparing to leave, and the night shift would not take over until midnight, well into the job. According to plan, the test should have been finished during the day shift, and the night shift would only have had to maintain decay heat cooling systems in an otherwise shut-down plant.
The night shift had very limited time to prepare for and carry out the experiment. A further rapid reduction in the power level from 50% was executed during the shift change-over. Alexander Akimov was chief of the night shift, and Leonid Toptunov was the operator responsible for the reactor's operational regimen, including the movement of the control rods. Toptunov was a young engineer who had worked independently as a senior engineer for approximately three months.
The test plan called for a gradual reduction in power output from reactor 4 to a thermal level of 700–1000 MW. An output of 700 MW was reached at 00:05 on April 26. However, due to the reactor's production of a fission byproduct, xenon-135, which is a reaction-inhibiting neutron absorber, core power continued to decrease without further operator action—a process known as reactor poisoning. This un-commanded continuing decrease in power occurred because in steady state operation, xenon-135 is "burned off" as fast as it is created from decaying iodine-135 by absorbing neutrons from the ongoing chain reaction to become highly stable xenon-136. However, when the reactor power was lowered, previously produced high quantities of iodine-135 decayed into the neutron-absorbing xenon-135 faster than the reduced neutron flux could burn it off. As the reactor power output dropped further, to approximately 500 MW, Toptunov mistakenly inserted the control rods too far—the exact circumstances leading to this are unknown because Akimov and Toptunov died in the hospital on May 10 and 14, respectively. This combination of factors rendered the reactor in an unintended near-shutdown state, with a power output of 30 MW thermal or less.
The reactor was now producing 5 percent of the minimum initial power level established as safe for the test. Control-room personnel decided to restore power by disabling the automatic system governing the control rods and manually extracting the majority of the reactor control rods to their upper limits. Several minutes elapsed between their extraction and the point that the power output began to increase and subsequently stabilize at 160–200 MW (thermal), a much smaller value than the planned 700 MW. The rapid reduction in the power during the initial shutdown, and the subsequent operation at a level of less than 200 MW led to increased poisoning of the reactor core by the accumulation of xenon-135. This restricted any further rise of reactor power, and made it necessary to extract additional control rods from the reactor core in order to counteract the poisoning.
The operation of the reactor at the low power level and high poisoning level was accompanied by unstable core temperature and coolant flow, and possibly by instability of neutron flux, which triggered alarms. The control room received repeated emergency signals regarding the levels in the steam/water separator drums, and large excursions or variations in the flow rate of feed water, as well as from relief valves opened to relieve excess steam into a turbine condenser, and from the neutron power controller. In the period between 00:35 and 00:45, emergency alarm signals concerning thermal-hydraulic parameters were ignored, apparently to preserve the reactor power level.
When the power level of 200 MW was eventually achieved, preparation for the experiment continued. As part of the test plan, extra water pumps were activated at 01:05 on 26 April, increasing the water flow. The increased coolant flow rate through the reactor produced an increase in the inlet coolant temperature of the reactor core (the coolant no longer having sufficient time to release its heat in the turbine and cooling towers), which now more closely approached the nucleate boiling temperature of water, reducing the safety margin.
The flow exceeded the allowed limit at 01:19, triggering an alarm of low steam pressure in the steam separators. At the same time, the extra water flow lowered the overall core temperature and reduced the existing steam voids in the core and the steam separators. Since water weakly absorbs neutrons (and the higher density of liquid water makes it a better absorber than steam), turning on additional pumps decreased the reactor power further still. The crew responded by turning off two of the circulation pumps to reduce feedwater flow, in an effort to increase steam pressure, and also to remove more manual control rods to maintain power.
All these actions led to an extremely unstable reactor configuration. Nearly all of the control rods were removed manually, including all but 18 of the "fail-safe" manually operated rods of the minimal 28 which were intended to remain fully inserted to control the reactor even in the event of a loss of coolant, out of a total 211 control rods. While the emergency SCRAM system that would insert all control rods to shut down the reactor could still be activated manually (through the "AZ-5" button), the automated system that could do the same had been disabled to maintain the power level, and many other automated and even passive safety features of the reactor had been bypassed. Further, the reactor coolant pumping had been reduced, which had limited margin so any power excursion would produce boiling, thereby reducing neutron absorption by the water. The reactor was in an unstable configuration that was clearly outside the safe operating envelope established by the designers. If anything pushed it into supercriticality, it was unable to recover automatically.
At 1:23:04 a.m., the experiment began. Four of the Main Circulating Pumps (MCP) were active; of the eight total, six are normally active during regular operation. The steam to the turbines was shut off, beginning a run-down of the turbine generator. The diesel generators started and sequentially picked up loads; the generators were to have completely picked up the MCPs' power needs by 01:23:43. In the interim, the power for the MCPs was to be supplied by the turbine generator as it coasted down. As the momentum of the turbine generator decreased, however, so did the power it produced for the pumps. The water flow rate decreased, leading to increased formation of steam voids (bubbles) in the core.
Because of the positive void coefficient of the RBMK reactor at low reactor power levels, it was now primed to embark on a positive feedback loop, in which the formation of steam voids reduced the ability of the liquid water coolant to absorb neutrons, which in turn increased the reactor's power output. This caused yet more water to flash into steam, giving yet a further power increase. During almost the entire period of the experiment the automatic control system successfully counteracted this positive feedback, continuously inserting control rods into the reactor core to limit the power rise. However, this system had control of only 12 rods, and nearly all others had been manually retracted.
At 1:23:40, as recorded by the SKALA centralized control system, an emergency shutdown of the reactor, which inadvertently triggered the explosion, was initiated. The SCRAM was started when the EPS-5 button (also known as the AZ-5 button) of the reactor emergency protection system was pressed: this engaged the drive mechanism on all control rods to fully insert them, including the manual control rods that had been incautiously withdrawn earlier. The reason why the EPS-5 button was pressed is not known, whether it was done as an emergency measure in response to rising temperatures, or simply as a routine method of shutting down the reactor upon completion of the experiment.
There is a view that the SCRAM may have been ordered as a response to the unexpected rapid power increase, although there is no recorded data conclusively proving this. Some have suggested that the button was not pressed, and instead the signal was automatically produced by the emergency protection system; however, the SKALA clearly registered a manual SCRAM signal. In spite of this, the question as to when or even whether the EPS-5 button was pressed has been the subject of debate. There are assertions that the pressure was caused by the rapid power acceleration at the start, and allegations that the button was not pressed until the reactor began to self-destruct but others assert that it happened earlier and in calm conditions.
After the EPS-5 button was pressed, the insertion of control rods into the reactor core began. The control rod insertion mechanism moved the rods at 0.4 m/s, so that the rods took 18 to 20 seconds to travel the full height of the core, about 7 meters. A bigger problem was a flawed graphite-tip control rod design, which initially displaced neutron-absorbing coolant with moderating graphite before introducing replacement neutron-absorbing boron material to slow the reaction. As a result, the SCRAM actually increased the reaction rate in the upper half of the core as the tips displaced water. This behavior was known after a shutdown of another RBMK reactor at Ignalina Nuclear Power Plant in 1983 induced an initial power spike, but as the SCRAM of that reactor was successful, the information was not widely disseminated.
A few seconds after the start of the SCRAM, the graphite rod tips entered the fuel pile. A massive power spike occurred, and the core overheated, causing some of the fuel rods to fracture, blocking the control rod columns and jamming the control rods at one-third insertion, with the graphite tips in the middle of the core. Within three seconds the reactor output rose above 530 MW.
The subsequent course of events was not registered by instruments; it is known only as a result of mathematical simulation. Apparently, the power spike caused an increase in fuel temperature and massive steam buildup, leading to a rapid increase in steam pressure. This caused the fuel cladding to fail, releasing the fuel elements into the coolant, and rupturing the channels in which these elements were located.
Then, according to some estimations, the reactor jumped to around 30,000 MW thermal, ten times the normal operational output. The last reading on the control panel was 33,000 MW. It was not possible to reconstruct the precise sequence of the processes that led to the destruction of the reactor and the power unit building, but a steam explosion, like the explosion of a steam boiler from excess vapor pressure, appears to have been the next event. There is a general understanding that it was explosive steam pressure from the damaged fuel channels escaping into the reactor's exterior cooling structure that caused the detonation that destroyed the reactor casing, tearing off and blasting the 2000-ton upper plate, to which the entire reactor assembly is fastened, through the roof of the reactor building. This is believed to be the first explosion that many heard. This explosion ruptured further fuel channels, as well as severing most of the coolant lines feeding the reactor chamber, and as a result the remaining coolant flashed to steam and escaped the reactor core. The total water loss in combination with a high positive void coefficient further increased the reactor's thermal power.
A second, more powerful explosion occurred about two or three seconds after the first; this explosion dispersed the damaged core and effectively terminated the nuclear chain reaction. However, this explosion also compromised more of the reactor containment vessel and ejected superheated lumps of graphite moderator. The ejected graphite and the demolished channels still in the remains of the reactor vessel caught fire on exposure to air, greatly contributing to the spread of radioactive fallout and the contamination of outlying areas.
According to observers outside Unit 4, burning lumps of material and sparks shot into the air above the reactor. Some of them fell onto the roof of the machine hall and started a fire. About 25 percent of the red-hot graphite blocks and overheated material from the fuel channels was ejected. Parts of the graphite blocks and fuel channels were out of the reactor building. As a result of the damage to the building an airflow through the core was established by the high temperature of the core. The air ignited the hot graphite and started a graphite fire.
There were initially several hypotheses about the nature of the second explosion. One view was that the second explosion was caused by hydrogen, which had been produced either by the overheated steam-zirconium reaction or by the reaction of red-hot graphite with steam that produced hydrogen and carbon monoxide. Another hypothesis was that the second explosion was a thermal explosion of the reactor as a result of the uncontrollable escape of fast neutrons caused by the complete water loss in the reactor core. A third hypothesis was that the explosion was a second steam explosion. According to this version, the first explosion was a more minor steam explosion in the circulating loop, causing a loss of coolant flow and pressure, that in turn caused the water still in the core to flash to steam. This second explosion then did the majority of the damage to the reactor and containment building.
However, the sheer force of the second explosion, and the ratio of xenon radioisotopes released during the event, indicate that the second explosion could have been a nuclear power transient; the result of the melting core material, in the absence of its cladding, water coolant and moderator, undergoing runaway prompt criticality similar to the explosion of a fizzled nuclear weapon. This nuclear excursion released 40 billion joules of energy, the equivalent of about ten tons of TNT. The analysis indicates that the nuclear excursion was limited to a small portion of the core.
Contrary to safety regulations, bitumen, a combustible material, had been used in the construction of the roof of the reactor building and the turbine hall. Ejected material ignited at least five fires on the roof of the adjacent reactor 3, which was still operating. It was imperative to put those fires out and protect the cooling systems of reactor 3. Inside reactor 3, the chief of the night shift, Yuri Bagdasarov, wanted to shut down the reactor immediately, but chief engineer Nikolai Fomin would not allow this. The operators were given respirators and potassium iodide tablets and told to continue working. At 05:00, however, Bagdasarov made his own decision to shut down the reactor, leaving only those operators there who had to work the emergency cooling systems.
The radiation levels in the worst-hit areas of the reactor building have been estimated to be 5.6 roentgens per second (R/s), equivalent to more than 20,000 roentgens per hour. A lethal dose is around 500 roentgens (~5 Gy) over 5 hours, so in some areas, unprotected workers received fatal doses in less than a minute. However, a dosimeter capable of measuring up to 1000 R/s was buried in the rubble of a collapsed part of the building, and another one failed when turned on. All remaining dosimeters had limits of 0.001 R/s and therefore read "off scale". Thus, the reactor crew could ascertain only that the radiation levels were somewhere above 0.001 R/s (3.6 R/h), while the true levels were much higher in some areas.
Because of the inaccurate low readings, the reactor crew chief Alexander Akimov assumed that the reactor was intact. The evidence of pieces of graphite and reactor fuel lying around the building was ignored, and the readings of another dosimeter brought in by 04:30 were dismissed under the assumption that the new dosimeter must have been defective. Akimov stayed with his crew in the reactor building until morning, sending members of his crew to try to pump water into the reactor. None of them wore any protective gear. Most, including Akimov, died from radiation exposure within three weeks.
Shortly after the accident, firefighters arrived to try to extinguish the fires. First on the scene was a Chernobyl Power Station firefighter brigade under the command of Lieutenant Volodymyr Pravik, who died on 9 May 1986 of acute radiation sickness. They were not told how dangerously radioactive the smoke and the debris were, and may not even have known that the accident was anything more than a regular electrical fire: "We didn't know it was the reactor. No one had told us."
Grigorii Khmel, the driver of one of the fire engines, later described what happened:
We arrived there at 10 or 15 minutes to two in the morning.... We saw graphite scattered about. Misha asked: "Is that graphite?" I kicked it away. But one of the fighters on the other truck picked it up. "It's hot," he said. The pieces of graphite were of different sizes, some big, some small, enough to pick them up...
We didn't know much about radiation. Even those who worked there had no idea. There was no water left in the trucks. Misha filled a cistern and we aimed the water at the top. Then those boys who died went up to the roof – Vashchik, Kolya and others, and Volodya Pravik.... They went up the ladder ... and I never saw them again.
Anatoli Zakharov, a fireman stationed in Chernobyl since 1980, offers a different description in 2008:
I remember joking to the others, "There must be an incredible amount of radiation here. We'll be lucky if we're all still alive in the morning."
He also said:
Of course we knew! If we'd followed regulations, we would never have gone near the reactor. But it was a moral obligation – our duty. We were like kamikaze.
The immediate priority was to extinguish fires on the roof of the station and the area around the building containing Reactor No. 4 to protect No. 3 and keep its core cooling systems intact. The fires were extinguished by 5:00, but many firefighters received high doses of radiation. The fire inside reactor 4 continued to burn until 10 May 1986; it is possible that well over half of the graphite burned out.
The fire was extinguished by a combined effort of helicopters dropping over 5000 metric tons of sand, lead, clay, and neutron-absorbing boron onto the burning reactor and injection of liquid nitrogen. The Ukrainian filmmaker Vladimir Shevchenko captured film footage of an Mi-8 helicopter as its main rotor collided with a nearby construction crane cable, causing the helicopter to fall near the damaged reactor building and killing its four-man crew. It is now known that virtually none of the neutron absorbers reached the core.
From eyewitness accounts of the firefighters involved before they died (as reported on the CBC television series Witness), one described his experience of the radiation as "tasting like metal", and feeling a sensation similar to that of pins and needles all over his face. (This is similar to the description given by Louis Slotin, a Manhattan Project physicist who died days after a fatal radiation overdose from a criticality accident.)
The explosion and fire threw hot particles of the nuclear fuel and also far more dangerous fission products, radioactive isotopes such as caesium-137, iodine-131, strontium-90 and other radionuclides, into the air: the residents of the surrounding area observed the radioactive cloud on the night of the explosion.
Equipment assembled included remote-controlled bulldozers and robot-carts that could detect radioactivity and carry hot debris. Valery Legasov (first deputy director of the Kurchatov Institute of Atomic Energy in Moscow) said, in 1987: "But we learned that robots are not the great remedy for everything. Where there was very high radiation, the robot ceased to be a robot—the electronics quit working."
I leave it here, if you want to find out what happens after this; click here and scroll down a little bit...
Wow! Scary to see the photos
Scroll down alot
@Luke92778 Thanks for understanding.
@Luke92778 Ok. I wasnt makong fun of you. I was distracted by my brother and forgot to add something saying I was just kidding. I feel bad now.
@Luke92778 It took you 10 minutes?!? My friend would laugh at you. He could read this in 3, maybe 4. 10 isnt that slow though.
@DarkLithium The internet can and will be a weird place. Have a nice day, and dont fall of the earth.
@SigmaTwelve Yep
@DarkLithium Nope, despite the buildings design, which is inferior to 99% of all other reactors of the era, it did not leave the reactor room in large amounts, it stayed most contained to a small radius. People still lived and worked inside, and close to the plant.
If there's one thing you can count on, it's humanities continued stupidness and ignorance, @DarkLithium
@SigmaTwelve Not really, still can't wrap my head around the amount of human error and straight stupidity...
@PINK From direct radiation poisoning casued by working at the plant at the time, being emergency services at the time, or being it the near by vicinity, I will say alot more people died earlier, or had some kind of effect..
Good for you, you figured out Chernobyl.
@DarkLithium only 50 died
@KnightOfAraluen Yeah. yeah. I know this! But it's also the internet.
@humangrenade Thanks :D
@PINK We won't have a number, I going to say more than 2000 people were harmed but shrugs shoulders we will never knpw
WHO and UN say only 2000 people, tops have had their live shortened. Even in the area around the plant, cancer is rare.
@DarkLithium legit wall of text, good job
Just pointing out the il part @DarkLithium
@DarkLithium A metaphor is used to compare two different people, animals, places, or things, or one from two different catagories. Example: She is a walking dictionary. That is the google definition.An oxymoron is saying something like oxymoron. An oxy is someone very smart. A moron is another word for idiot. Dont take me wrong and think I am trying to be mean. I am just giving useful, or not useful, information.
@KnightOfAraluen It's meant to be ironic, and a metaphor...
If someone is illiterate, which is who you wrote this for based on the title, they couldnt read this anyways. Also, an illiterate nerd is kind of an oxymoron. Just teasing btw. dont take the first part seriously.
@General360 Well it the accident started today...
@Upquark IL litterate?
if we are IL litterate, we cant read...